Failure investigations of a first stage Ni based super alloy gas turbine blade

2016-10-25_17h11_11A paper presented at the « International Conference on Processing of Materials, Mineral and Energy », 29th and 30th july 2016, PACE Institute of Technology & Sciences, India. It had been published by Elsevier.

This paper deals with the failure investigations of the first stage gas turbine blade of 30MW gas turbine. This blade is manufacture with of nickel based super alloy IN738. The main focus of the paper is to found the causes of failure of the blade. By the investigations, it is found that the blade failure takes place due to the combined effect of erosion, oxidation, overheating, and hot corrosion.

More at : http://www.pmme.co.in/papers/EMT-087.pdf

Investigation of Minor Leakage in a Fuel Oil Return Line

A small fuel oil return line of a stationary gas turbine engine failed by high cycle fatigue cracking. In the metallurgical root cause investigation, performed by the original equipment manufacturer’s laboratory, it was determined that insufficient support of the fuel line and the ensuing vibration led to dynamic alternating bending stresses, that had their maximum immediately adjacent to the connector weld of the flange…………. Read more