The discussion of this paper will focus on the H1 Trench COTA bushing, which failed after field maintenance handling that would not normally be expected to have a negative effect on a bushing. Following the failure, the top air side porcelain was found ruptured and missing; the bottom insulator was fractured into a number of pieces. The H2 and H3 bushings from this transformer, which were identical Trench type bushings, were also removed and disassembled for inspection to help identify a possible root cause of the H1 bushing failure.